AREA: LOUISIANA
Jar Data from “SPARTAN THRU TUBING” (JEFF MILLER)
10/17/111.Job Objective: “To fish out stuck 16′ slickline tools” Fluid Type: 4% KCL Fluid Wt: 8.5# BHT: 300*
Deviation: 17 degrees Jar OD: 2 1/8″ Jar Licks (10,000-20,000#) =1 Conclusion: Pulled Fish Free
10/21/2011
2.Job Objective: “To fish out PX Plug” Fluid Type: 4% KCL Fluid Wt: 8.5# BHT: 300*
Deviation: 15 degrees Jar OD: 1 11/16″ Jar Licks (5,000-10,000#) =26 puh/48 cycle out
Conclusion: pulled fish loose/puh hung up in next nipple
12/24/2011
3.Job Objective: “To fish out 180′ thru tubing gravel pack screens” Fluid Type: Brine Fluid Wt: 10.5#
BHT: 250* Deviation: 26 degrees Jar OD: 1 11/16″ Jar Licks (5,000-10,000#) =6
Conclusion: pulled fish free
2/6/2012
4.Job Objective: “To fish out 28′ stuck eline setting tool bha” Fluid Type: Brine Fluid Wt: 9.7#
BHT: 310* Deviation: straight Jar OD: 2 7/8″ Jar Licks (10,000-20,000#) =1 (20,000-30,000)=1
Conclusion: pulled fish free
3/18/2012
5.Job Objective: “To fish out 38′ stuck eline guage ring tools” Fluid Type: 4% KCL Fluid Wt: 8.5#
BHT: 320* Deviation: 20 degrees Jar OD: 2 7/8″ Jar Licks (10,000-20,000#) =2 (20,000-30,000)=1
Conclusion: Broke cablehead off of fish
4/23/12
6.Job Objective: “Milling Job/got hung up on gas lift valve pooh” Fluid Type: 4% KCL Fluid Wt: 8.5#
BHT: 300* Deviation: 15 degrees Jar OD: 1 11/16″ Jar Licks (5,000-10,000#) =15
Conclusion: Fired both ways/stayed stuck/disconnect
4/26/12
7.Job Objective: “To fish out 36′ of stuck eline guage ring tools” Fluid Type: Oil base Mud Fluid Wt: 16.0#
BHT: 320* Deviation: 20 degrees Jar OD: 2 7/8″ Jar Licks (10,000-20,000#) =10 (20,000-30,000)=27
Conclusion: Broke grapple in overshot
4/27/2012
8.Job Objective: “To fish out 36′ of stuck eline guage ring tools” Fluid Type: Oil base Mud Fluid Wt: 16.0#
BHT: 320* Deviation: 20 degrees Jar OD: 2 7/8″ Jar Licks (10,000-20,000#) =5 (20,000-30,000)=25
Conclusion: Pulled Fish free